Icelandic Test Smelt One - Stone Plate and Blow Hole
October 7, 2007
Smelt Team: Darrell Markewitz and Neil Peterson.
Smelter Construction:
To clearly distinguish the lower base level (basically just support), a layer
of heavy brown paper was laid down over the area. It was not expected any liquid
slag or excessive heat would penetrate down to this level. The paper allows
clearly visible separation at the lower ground supporting the structure. At
the same time should any hot liquid slag penetrate this far, the paper will
not halt its downward movement.
A new artificial ground level was established above this. Raw earth from elsewhere
in the yard was laid roughly level and compacted (using a brick as a mallet)
to a depth of 10 cm. To contain this layer a line of heavy clay bricks was positioned
just proud of the existing line of concrete blocks. This construction gives
enough space to build up the stone front for the clay cobb cylinder of the smelter.
There are a number of flat stone slabs of various compositions and sizes on
hand from earlier gathering trips. Neil had gathered a donation of pre-mixed
pottery clay (donated by Potter Supply House in Kitchener). This was cut into
slabs roughly 6 cm thick, each trimmed to allow them to be stacked into the
cylindrical shape of the smelter. The seams were 'mortared' using the waste
'smelter clay' that Selena has provided.
At the front of the smelter, the structure was built up from stone slabs. The
lower section was raised to a level of roughly 20 cm. Two smaller pieces were
laid on top of this, leaving a central slot about 5 cm wide by 7 cm high. On
top of this was placed a large slab - 4 cm thick by roughly 30 cm tall, which
was 30 cm at the lower edge and 20 cm at the upper. This slab sat over the zone
of the smelter that is subjected to the highest operating temperatures.
The tuyere was mounted so that the tip of the steel pipe was set to just even
with the inside surface of the smelter (the edge of the upper stone slab. For
this experiment, the standard 22 1/2 down angle was used. Air was delivered
via our standard blower, with the rate in the higher volume range that has proved
successful in our earlier smelts.
The smelter was constructed on Saturday, and left for the moisture inside the
clay to at least partially stabilize over night. This step turned out not to
be as effective as was hoped.
Because of the use of block clay (in replace of the standard cobb mixture) a
longer than normal preheat sequence was undertaken. Split wood was burned using
natural draw for about 1 1/2 hours. A low air blast was then applied for a further
25 minutes before filling with charcoal to begin the primary sequence. The higher
temperatures created by the air blast to the wood drastically effected the clay.
As the internal dampness flash heated to steam, serious spalling (in fact explosive
shattering) of the clay bricks was the result. This so seriously damaged the
top course of the clay blocks that this layer was removed and then replace with
the sheet metal cylinder used in past smelts. This allowed us to maintain the
normal working height of the smelter (adjusted total was 60 cm above the tuyere)
For this smelt, there was not a fixed base of charcoal fines established at
an optimum level. Instead, the bottom of the furnace (packed earth) was allowed
to accumulate a layer of ash and charcoal from the pre heat materials. In the
end this would effect the position of the developing bloom.
Although the smelt was started with a reduced air volume, we fairly early on
decided to return to more familiar methods - so increased the air delivery to
the range of 600 litres per minute. With this higher air flow the charcoal consumption
was in the range of 8 - 5 minutes per standard bucket.
The ore used was the commercial hematite grit. To reduce the tendency of this
smaller particle size to absorb excess carbon in the reaction zone, the ore
was added as a single scoop sized slug, spread evenly over the top of the smelter
each time (as opposed to layering it through out each charcoal bucket). It was
decided to aim for a historic sized bloom, so a rough total of 11 kg of ore
was used.
The primary smelt sequence (first charcoal to extraction) took about four hours.
A top extraction was undertaken, again represented the process we expected may
have been used in the archaeological setting we are working towards. There was
a clear knob of slag produced at the tuyere which was certainly melted stone
from the front slab. This turned out to be a different composition than the
normal slag bowl material - with a significantly different melting temperature.
The slag bowl and bloom had also formed somewhat lower in the furnace than has
been the case in the past. Both these results made finding and extracting the
bloom a bit trickier than in past experiments.
In the end, Neil pulled the resulting bloom. The weight was about 6 kg (roughly
45% return). As has been the case with other uses of the hematite ore, the exterior
of the mass was fairly crumbly, but with a clearly solid core.
The theoretical layout for the test smelter |
Details of the lower base level. | Smelter Construction details - front elevation |
Working set up - side elevation |
Initial Construction of Smelter
The remains of the last smelt removed, new floor level filled with ash / sand / debris mix. | Layer of heavy brown paper laid to mark floor level | New base level established using packed soil, retained by line of bricks. |
Lower area of front smelter built up of stone slabs to a height of about 20 cm. Bricks to sides are not part of smelter, but used to retain earth fill to be added later. | Commercial potter's clay cut into roughly 6 cm thick slabs will make up the body of the smelter. | Showing the clay slabs laid in to the first (slag bowl) level. Soft waste clay was used as a mortar to seal the slabs together. |
Rectangular stones establish the blow hole space roughly 5 cm wide by 7 cm tall. Second row of clay slabs in place | Fitting the stone front plate in place. The stone slab was roughly 4 cm thick and extends about 20 cm across and about 30 cm above the blow hole. | A view from the top of the smelter, showing the fitting of the stone front plate. A mix of ash / sand / debris is used as back fill to stabilize the smelter. |
A closer view of the inside of the smelter. The blow hole is just below the dark grey surface of the front stone plate. | The finished construction. |
Firing the Smelter
Starting the pre-heat using split wood. Unlike earlier smelts, there was not a base set with charcoal fines. | The pre-heat continues with the bellows tube and air system in place. The tip of the steel pipe bellows tube is set just even with the interior wall surface of the smelter. | Short drying time for the solid clay left considerable moisture remaining. The result was serious spalling and cracking of the clay slabs, particularly at the top of the smelter. |
As the pre-heat continues, the base area below the blow hole fills with ash and small charcoal. | Because of the excessive cracking of the top layer of clay slabs, this layer was removed and replaced with a metal cylinder. | With the open blow hole and high volume air, a significant amount of the blast merely blew back from the mount of the bellows tube. This image taken just after the first filling of the smelter with charcoal. |
About 35 minutes into the main smelt sequence, the first drip of slag is seen at the blow hole. | Fairly quickly, dripping slag solidifies across the blow hole, effectively sealing the bellows tube into a tuyere even with the inner surface of the smelter wall. | Neil attempts a 'down the kilt' shot of the inside of the smelter. Although the air blast is now sealed inside the smelter, the heat radiating off the stone slab was significant. |
Nearing the end of the smelt. Note the colour of the stone slab above the tuyere. | Into the burn down phase. The volume of charcoal in the upper metal cylinder has been consumed, so that had been removed. | The charcoal level is allowed to burn down to just about the tuyere level. This image just before the remainder of burning fuel is scooped out to expose the hot bloom in its bath of liquid slag. |
Continue for the EXPERIMENT
DATA |
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The resulting 6 kg bloom just after some of the loose mother has been hammered off. Less compaction of the surface has been accomplished than normal - due to the exhaustion of the workers! | Just after the smelt. Some of the clay slab walls have fallen into the still hot interior. These were broken away during the extraction effort. The cooling bloom can be seen to the upper right. | Smelt in Progress Quicktime Movie (1.9 Mb) |
Excavating the Smelter Remains