OABA May Meeting May
14, 2005
Experiment Notes - ECONONORSE Smelter
Leader : Darrell Markewitz
Assisting: Neil Peterson / John Burton
Recorder
: Neil
Peterson / Vandy Simpson
Charcoal Monkeys: Gus
Gissing / Ken Cook / Sam Falizone
TIME EVENT MEASUREMENT
Relative Elapsed Relative Absolute Total
Fuel Ore
-00 00 start
preheat with wood splits
-35 35 addition
rough charcoal, gentle air blast
-45 45 fill
with rough charcoal
12:00 00 timer
reset - smelt begins
12:10 10 first
measured charcoal 1 4
lbs* 4 lbs
12:20 10 charcoal 2 8
lbs
12:40 20 charcoal 3 12
lbs
12:51 11 seed
charge 1 .75
lbs .75
lbs
charcoal 4 16
lbs
1:06 15 seed
charge 2 .75
lbs 1.5
lbs
1:09 18 charcoal 5 20
lbs
1:32 23 charcoal 6 24
lbs
26 seed
charge 3 .75
lbs 2.25
lbs
1:40 addition
of second hand crank blower
1:45 tuyere replaced with copper
***
2:02 30 charcoal 7 28
lbs
seed charge 4 .75
lbs 3
lbs
2:12 10 charcoal 8 32
lbs
2:17 15 seed
charge 5 .75
lbs 3.75
lbs
2:29 17 charcoal 9 36
lbs
12 seed
charge 6 .75
lbs 4.5
lbs
2:44 15 charcoal 10 40
lbs
15 seed
charge 7 .75
lbs 5.25
lbs
2:49 5 charcoal 11 44
lbs
5
seed
charge 8 .75
lbs 6
lbs
2:53 4 charcoal 12 48
lbs
4 full
charge 9 1.5
lbs 7.5
lbs
3:00 7 charcoal 13 52
lbs
3:10 17 half
charge 10 .75 lbs 8.25
lbs
3:12 12 charcoal 14 56
lbs
2 full
charge 11 1.5 lb 9.75
lbs
***
3:23 11 charcoal 15 60
lbs
full charge 12 1.5 lb 11.25
lbs
3:31 12 charcoal 16 64
lbs
full charge 13 1.5 lbs 12.75
lbs
3:38 7
charcoal 17 68
lbs
full charge 14 3 lbs 15.75
lbs
3:50 12 charcoal 18 72
lbs
full charge 15 3 lbs 18.75
lbs
3.58 8 charcoal 19 76
lbs
full charge 16 3 lbs 21.75
lbs
4:11 13 charcoal 20 80
lbs
full charge 17 2.25 lbs 24
lbs
4:21 first
tapping attempt
4:23 12 charcoal 21 84
lbs
half charge 18 .75 lbs 24.75
lbs
4:26 3 charcoal 22 88
lbs
full charge 19 3.75 lbs 28.5
lbs
4:36 10 charcoal 23 92
lbs
full charge 20 2.25 lbs 30.75
lbs
second tapping attempt
4:44 12 charcoal 24 96
lbs
full charge 21 2.25 lbs 33
lbs
4:52 12 charcoal 25 100
lbs
full charge 22 2.25 lbs 35.25
lbs
5:02 10 charcoal 26 104
lbs
full charge 23 3 lbs 38.25
lbs
5:15 13 charcoal 27 108
lbs
full charge 24 2.25 lbs 40.5
lbs
5:22 7 charcoal 28 112
lbs
full charge 25 3 lbs 43.5
lbs
5:32 10
charcoal 29 116
lbs
full charge 26 3.75 lbs 47.25
lbs
5:43 11
charcoal 30 120
lbs
full charge 27 3 lbs 50.25
lbs
5:54 11 charcoal 31 124
lbs
full charge 28 3 lbs 53.25
lbs
6:08 12
charcoal 32 128
lbs
full charge 29 3.75 47
lbs
6:29 tap
slag and recycle 3
lbs ´
(one charcoal addition may be missing here)
6:34 26 charcoal 31 132
lbs
6:43 11 charcoal 32 136
lbs
6:52 11 charcoal 33 140
lbs
6:59 7
charcoal 34 144
lbs
7:06 7 charcoal 35 148
lbs
7:13 start
to dismantle smelter
7:26 bloom
removed
NOTES:
All ore
charges are based on a Ôstandard scoopÕ - taconite weight of .75 lbs
* All charcoal charges are
based on a Ôstandard pailÕ - weight of 4 lbs
´ This is estimated
weight only, not added into charge total
*** Marks
areas were records are suspect
YIELD: 21 lbs
(estimated)
This
represents 45 % yield from roasted ore weight
Bloom was
significantly ÔtroughÕ shaped - this a result from changes in the tuyere angle during the smelt. Weight estimate is for the
main bloom only, and does not include smaller (walnut sized) fragments. Roughly
one third of the mass was cut off while still hot from the smelt. The remaining
section weighs 14 lbs.
Considerable
trouble was experienced during the early part of the sequence with air
delivery. Although checked before storage, the main blower did not work at
first attempt. A smaller (less volume) vacuum blower was initially employed.
Concern developed that it was not producing enough air volume, so a second hand
cranked blower was added in conjunction. The main blower was checked and
re-installed to the smelter about hour three.
The use of
a packing mixture of roughly 50 / 50 beach sand and rough saw dust proved a
mixed blessing. First, gaps in the brick structure were not sealed with clay.
During firing, the sawdust element burned, and the heated sand ran like a fluid
through the cracks. Continual addition of replacement packing proved necessary.
As it
turned out, the pure taconite ore lacked the silica content to provide for the
required slag. Normally this would have been a major problem, as the firebrick
adds little silica (through melting). In this smelt, the sand from the packing
actually added the required silica content to create plentiful slag - required
to control the carbon content of the bloom.
One third of the bloom
was given to Lloyd Johnson. He latter consolidated and finished the mass into a
workable bar. He reports that the material created was Ônice soft workable ironÕ.
2021 Note : This report was
recovered from a much older software version. For this reason the formatting is
less than ideal.