Vinland 4 - June 12, 2010
   Working towards a reconstruction of the L'Anse aux Meadows Smelt
  
   Smelt Report
  This smelt was primarily a test of presentation method of the Vinland smelt, 
  part of the general dress rehearsal in preparation for DARC's demonstration 
  event at L'Anse aux Meadows NHSC, August 15 - 25, 2010. Primarily intended as 
  a demonstration, it was undertaken using only Viking Age tools, and in Norse 
  clothing. The construction of the smelter and the layout of the working space 
  was the same as that indicated by the archaeology of L'Anse aux Meadows. (Details 
  of the logic behind this series)
  
  The working team was :
  Darrell Markewitz - construction / smelt master
  Ken Cook - lead hand
  Sam Falezone & Pierre La Fountaine - bellows
  Images are by David Cox
  One of the primary concerns with working against the LAM evidence is that the 
  furnace construction is a simple clay and sand mix. Our own past experience 
  with this material has almost always resulted in heavy cracking to the furnace 
  walls. (Although it should be noted that others, especially Sauder & Williams 
  do NOT have that problem!) This was certainly the case in this experiment.
  This smelt was also predicted to have lower yields than our usual.
  First, the ore analog mix used thought to be part of the reason. The analog 
  used here was a blend of Spanish Red oxide and Hematite grit.
  The main reason that low yields are predicted for these smelts is the method 
  of air delivery - use of the human powered Norse double bag bellows. The air 
  volume available is based on a theoretical delivery, the there has proved to 
  be large variation in delivery between individual operators.
  

Theoretical Layout
  The physical layout of the equipment is based not only on the archaeology, but 
  also how that evidence has been interpreted by the working smelt team based 
  on its past experience. 
  With the remains of the smelter base placed slightly to one side of centre, 
  the bellows has been positioned to the wider side (the left as seen here). Use 
  of a leather Y coupling allows for just enough room to permit clearing of the 
  tuyere as required. The evidence suggests a tap arch towards the open front 
  of the structure. The large pit to the front left is interpreted here as the 
  stable mounting of a wooden stub to hold a large stone anvil for the consolidation 
  step. Through some luck, a large stone with relatively flat surfaces had been 
  found that was fairly close to that found at LAM to serve as this anvil. The 
  pile of charcoal was placed to the right rear, and ore addition to the right 
  centre. A slack tub placed to the right front corner cools working tools close 
  to hand.

Bellows Operator view, from the rear left corner out the open front 
  of the working space. (Before drying fire in furnace.)
  As with other furnaces in the Vinland series, the walls were built up of a simple 
  clay and beach sand mix, at roughly 50 / 50. The starting interior diameter 
  was 23 cm (9 inches), produced by using a metal form wrapped in newspaper. Wall 
  thickness initially was roughly 5 cm. The furnace was constructed on top of 
  a circle of fine white silica sand (to help distinguish this experiment from 
  earlier ones). As each course of clay was built up, the form would be removed, 
  and the interior filled with a dry mix of wood ash and beach sand (also a 50 
  / 50 mix). This helped to stabilize the structure, speed drying of the clay, 
  and allow the form to be raised for the next clay course.

First course completed 
  with packing added - note the shape is cylindrical at this point.
  As the construction continued, it became apparent that the first batch of clay 
  had been mixed up a bit too wet. Despite considerable care to prevent downwards 
  force as the next two upper courses were applied, the base level started to 
  slump under the weight. The end result of this was not only a thickening of 
  the lower wall, but also a considerable belling outwards. The end result was 
  a pronounced 'pot belly' shape instead of the normal cylindrical or tapered 
  shaft. This increased the diameter of the smelter to closer to 28 cm (11 inches) 
  at tuyere level. 
  As ideal air volume is related to cross section area at that point, it was expected 
  that there might not be enough air produced by the Norse bellows. Such lowering 
  of available air was expected to also lower potential bloom yield. At the intended 
  diameter of 20 - 22 cm the ideal air volume would be 500 + litres per minute. 
  Expanded to 28 cm the ideal air increases to closer to 1000 + litres per minute. 
  (This is well beyond the ability of the test 
  bellows to produce.) 
  Although the initial build was to roughly 65 cm, the slumping reduced this height 
  to closer to 60 cm. The next day an extra layer was added to the top of the 
  walls to extend these to roughly 68 cm (26 1/2 inches).

Measurements of the completed 
  furnace.
  
Cut out Tap Arch, showing increase in wall thickness at base to about 10 cm 
  - due to slumping.
  
Furnace with tuyere set in place, showing final shape after slumping of the 
  walls (just before pre-heat)
  A small tap arch was cut into the base, 20 cm wide by 14 cm tall. This was separated 
  from the parent wall with a thin layer of birch bark to keep it from re-sealing. 
  
  The tuyere was forged from mild steel pipe (standard schedule 40). A taper was 
  created over roughly the last 10 cm, reducing the starting interior diameter 
  from 3.5 cm down to 2 cm at the tip. A series of three sewn leather tubes, held 
  tightly in place with thongs, jointed the tuyere to the bellows tube. The effect 
  of these leather couplings was two fold. First their flexibility reduced any 
  vibration or movement from the working of the bellows from being transmitted 
  to the tuyere mounted in the fragile smelter wall. The second effect was to 
  prevent heat absorbed by the metal pipe from being radiated back up the system. 
  In the centre of the couplings was a leather Y tube, the last branch filled 
  with a tapered wooden plug. Removing this plug allowed to probe down through 
  the tuyere to clear any blockages as might be required. Overall this system 
  proves quite stable and effective.
  The tuyere itself was set up as has been proven to be the ideal through past 
  experiments. It angled downwards at 22 1/2 degrees, protruding into the smelter 
  5 cm proud of the inner wall. The centre of the tip was positioned 19 cm above 
  the ground level base of the furnace.

View of the interior after the initial 
  drying fire. Note large crack extending down to the right of the tuyere.
 This was the crack that would cause problems later in the smelt
  The night before the smelt, the normal small drying fire of wood splints was 
  started inside the furnace. Four to six pieces of hardwood, split down to roughly 
  thumb diameter, were added at a time. The drying process was conducted with 
  primarily natural draft caused by slightly pulling back the tap arch block. 
  The bellows was only used when the fire was in danger of completely going out. 
  The process heated through to the exterior, making it 'almost too warm to hold 
  your hand to'. After about three hours, a metal cap was placed over the top 
  of the furnace, and the coals inside were allowed to burn down to ash (as seen 
  in the image above, taken the next morning). 
  It was discovered there were several large cracks which ran from the top of 
  the furnace right down to the base. The largest of these was opened up to about 
  1 cm at the top. As the initial pre-heat fire of wood splints was started, an 
  attempt was made to use what little softened clay remaining on hand to wedge 
  shut these cracks. As the damp clay was sure to shrink and crack itself, it 
  was only expected to reduce, but not eliminate, the effects the large cracks 
  would have on the progress of the smelt.
 
At the start of the pre-heat, stone 
  slabs packed with ash and sand mix.
  As with other furnaces in the Vinland series, the clay inner liner was surrounded 
  by a series of flat stone slabs. The clay core of the furnace would certainly 
  have endured a single firing event without any additional support. The primarily 
  function of the slaps is actually to hold a layer of packing material in place, 
  the same 50/50 mix of wood ash and sand used during construction. On exposure 
  to the high temperatures of the smelter, this mix actually will form a simple 
  glass, which also will help to plug cracks. If the holes become over large, 
  the packing will run into the inside of the smelter, which can result in excessive 
  slag formation. This itself can cause problems with managing the smelt.
  As the first load of rough charcoal was added, there was considerable problems 
  with explosive spalling, especially at the outer top areas of the clay walls. 
  New cracks developed, existing ones widened. 
  The conduct of the smelt was based entirely on past experience, the look and 
  sound of the working smelter, rather than objective measurements of time and 
  temperature. All the workers had past bellows experience, both at the smelter 
  and as working blacksmiths. This allowed there to be a relatively constant supply 
  of air over the entire progress of the smelt. This despite switching operators 
  every 10 minutes or so, and individual fatigue over the roughly four hours of 
  the smelt. Consistency of air delivery was based mainly on sound, as individual 
  operators had differing styles of stroke. Delivery produced is a combination 
  of length of the stroke, frequency of the stroke, plus amount of force used 
  for the stroke. For most operators, one stroke is required each second, roughly 
  the rhythm of a healthy heart's beat.
  A wooden scoop had been made of green birch wood, of a size to hold about a 
  'double handful' of ore. Earlier measurements of the Dark Dirt analog showed 
  that the average weight of a slightly rounded scoop full was 540 gms.
  The total amount of ore had been pre-measured to 20 kg of the Dark Dirt 1A analog. 
  In fact this amount 'filled to heaping' the wooden bucket set aside to hold 
  the ore. This material contained a combination of Spanish Red oxide and granular 
  Hematite. The available Fe content was calculated 
  to be 55% 
  Charcoal was added by 'a standard bucket'. A wooden bucket had been marked to 
  contain the same volume as our standard (modern) bucket, which contains about 
  1700 gms of sized, dry charcoal. 
  Besides attempting to maintain a constant air flow, the only other control was 
  the distribution of ore additions related to charcoal consumed. Again the pattern 
  used was based on experience gained from past smelts. The entire interior of 
  the smelter to come up to full temperature, when the glowing orange of ignited 
  charcoal climbs to a level about 40 - 45 cm above the tuyere (about 7 cm below 
  the top). At this point ore is added, distributed evenly through each bucket 
  load of charcoal. The first four additions of ore consisted of single scoop 
  measures per bucket of charcoal. The next three charcoal measures included 2 
  scoops. The next two additions included 3 scoops. The last bucket included the 
  remaining ore, just over 3 scoops. 

Late in the smelt. Gases escaping from the 
  widening cracks are evident.
  The stone slabs have been re-positioned several times in an attempt to plug 
  the worst of the gaps.
    Image by David Cox
  
  It only proved necessary to tap liquid slag once during the main sequence. This 
  was roughly 2/3 the way through the process. The tapping was done through the 
  front arch, moving the block away and punching a small hole through the slag 
  bowl on the side away from the tuyere. Generally the tuyere worked cleanly, 
  clearing slag obstructions was only required a couple of times. The impression 
  was that the higher pressure pulses of air produced by the direct stoke with 
  the Norse double bag bellows was assisting to keep the tuyere clear. 
  It had been expected with the various cracks that developed that the furnace 
  would self tap. This proved not to be the case through the bulk of the smelt. 
  A dramatic event near the end of the main sequence was to alter the course of 
  the smelt.
  The last charge of ore, about 3 1/2 scoops, had been added. One last full bucket 
  of charcoal had been added to cover this, and the burn down had begun. The top 
  level of charcoal had dropped down about 10 cm. At this point the last ore addition 
  would have fallen to roughly just above tuyere level. Suddenly, a massive pour 
  of slag vented out of the crack just to the side of the tuyere (towards the 
  rear, away from the tap arch). There was a bit of a mad scramble in an attempt 
  to halt this flow. (I was working the public rope line outside the smelter when 
  this happened). In the end approximately a litre or more of liquid slag was 
  lost. 
  The first, and likely most important result was a considerable drop in internal 
  temperature within the smelter. As soon as the iron rich slag had cooled enough 
  to allow it to be picked up, pieces were returned back into the smelter, along 
  with about another half bucket of charcoal. The hope was that this material 
  would melt, and some of the iron it contained would be deposited to the developing 
  bloom. This certainly proved not the case, as the furnace had lost enough heat 
  that those pieces never did melt. 
  The regular burn down continued, to a point there was perhaps 10 - 15 cm of 
  charcoal remaining above the tuyere / slag bowl level. The normal top extraction 
  method was used : reducing air flow, scooping out the remaining charcoal to 
  uncover the top of the slag bath, hammering the top of the bloom in place with 
  the wooden log 'thumper'. The bloom with its usual loose coating of 'mother' 
  was pulled free easily with the bloom hook, then grabbed with the bloom tongs 
  and moved to the stone anvil.
 
    Working the bloom, near the end of the consolidation step. 
  Note the pile of loose 'mother' scattered on the stone anvil.
    Image by David Cox
  As the bloom was pulled from the smelter, it was immediately obvious that the 
  mass was significantly less that what has been come to be expected from earlier 
  smelts. Our normal practice is to lay the bloom directly on the top of a wooden 
  stub, rather than employing any kind of anvil. Lack of experience working on 
  a stone anvil caused the incorrect assumption to be made of the blooms character. 
  The dull 'whack' sound on each hammer stroke was so like the sound of hitting 
  cast iron, this was pronounced to be the quality. In retrospect, the mass was 
  also considerably colder than is normal, even as it was pulled from the furnace. 
  In the past the newly extracted bloom is closer to a 'bright yellow' welding 
  heat. In this case the metal was a best a 'bright orange'. As it was hammered, 
  it was just not hot enough to be welded up, but instead was more mechanically 
  compressed. The result was a brick shape, containing a lot of cracks. 
 
Partially 
  compressed bloom, what was likely the upper face when inside the furnace. 
  The mark from the grinding test can be seen.
  The total size was 12 x 6 x 4.5 cm, weight at 1400 gm, with a second small irregular 
  piece at about 150 gm. With a total starting weight of ore at 20 kg, that equals 
  a yield of only 8%. Far less than expected! A later spark test on the centre 
  face of the brick suggests a nice low carbon iron.
   Some valuable comments:
  Kevin Smith reminded me (again) of one of the truisms of archaeology 
  : that 'absence of evidence is not evidence of absence'.
  " The preserved thickness of fragments of the walls of a smelting furnace 
  may only be telling you how far intense heat penetrated into the unfired clay 
  of the original walls and fired it into a more durable ceramic. In other words, 
  the "as built" walls may have been far thicker but the outer surfaces, 
  being less intensely fired or still semi-raw, may well have eroded completely 
  and washed away into the soil matrix at the site. ...
  " In other words, without seeing the original, actual samples from 
  L'Anse aux Meadows, I would not put much trust in reconstructing a tapered wall 
  thickness from 10 cm (base) to 5 cm (top)...unless the actual original pieces 
  from L'Anse aux Meadows are so well preserved that it's clear that all of them 
  have well-preserved exterior and interior surfaces. If they do not, then what 
  the L'Anse aux Meadows published furnace wall fragments are actually telling 
  you is ONLY that the furnace walls were *at least 10 cm thick*. I do not think 
  you can assume that they were any thinner unless they do have furnace wall fragments 
  just 5 cm thick with well-preserved and distinct finished surfaces on both sides. 
  "
  Lee Sauder (and others) have clarified the value of sand in 
  the construction of walls:
  " You need to make sure you're using a good clay, it needs to be heavily 
  grogged with sand or clay grog, it needs to be mixed properly (not too much 
  water), it needs to be worked and kneaded (wedged), and it should rest before 
  you use it.
  ...
  " The organic fibers are nice, but if you can't use them, just increase 
  the sand or grog so that your clay content stays low. The sand doesn't change 
  size much when it gets hot, the clay does. "
   Conclusions:
  
  In retrospect, the use of unknown clay, a choice caused by simple time pressures 
  and supply problems, appears to be the main cause of the construction problems 
  with this furnace itself. This statement based on the fact that this there were 
  three other furnaces constructed earlier on the same layout, and the methods 
  employed were those fairly standard for the building of many others. With the 
  new clay the only major variable, this certainly appears to be the source. My 
  plan for the actual LAM demonstration smelt is to have enough of of standard 
  clay on hand for the build. There remains the possibility of acquiring enough 
  of the local clay to build the furnace of. This however would then add a second 
  level to the experiment itself.
  Some better understanding needs to be acquired on the effects of various mixtures 
  of sand and clay. I had originally thought that mixing 50 % sand was a generous 
  amount, but the advice given based on the direct experiences of others suggests 
  this is not the case. Without definite knowledge of the exact mixtures utilized 
  at LAM originally, this all remains guess work at best. The furnace used for 
  Vinland 4 did experience hardly any interior wall erosion, normally a significant 
  concern on at least the first firing of such small clay wall furnaces. A number 
  of others have explained that increasing sand or adding grog normally helps 
  *prevent* cracking. Generally this was linked to problems during the actual 
  firing cycle of the furnace, which was not the case here. Since the cracking 
  developed during the initial drying, some modification of that method should 
  be considered.
  The exact composition of the ore used was not recorded. It was however a mixture 
  of our DD1 (red) plus some amount of granular hematite. The straight DD1 (at 
  45% Fe) has proven to produce lower yields (in the range of 15%) in the past, 
  so perhaps the low yield on this experiment should have not been so unexpected. 
  The addition of any amount of hematite (at 68% Fe) could have only served to 
  enrich this ore.
  There has been some indication that it may be possible to utilize locally gathered 
  primary bog ore for the LAM demonstration smelt. My plan is to bring enough 
  of the previously tested DD2 (black) analog. Switching to an unknown and untested 
  ore is most likely to modify the entire theme of the LAM smelt from 'practical 
  demonstration' into 'experimental archaeology'. Consultation with Parks Canada 
  would certainly be called for before switching the focus.
  The other large variable most likely to impact bloom formation is the air system. 
  As has been indicated, the working volume of the Norse type smelting bellows 
  may not have been adequate to produce enough air, considering the expansion 
  of the slumping furnace from the planned 22 cm to 28 cm internal diameter. Low 
  air almost always equals low yields and less dense blooms, both of which occurred 
  in this experiment. The other use of the same human powered system (Vinland 
  3) also resulted in lower yields than expected, despite the use of a significantly 
  higher iron content ore. It is hoped that with more practice (and a solid working 
  team) fluctuations in delivery (thus temperatures) can be leveled out.
      
   Text and photography © 2010, 
  Darrell Markewitz 
  Images by David Cox are indicated